Open
Conversation
update from arduino head
Prior to seeing the pulse start, the timeout would tick by at 16/11ths of the speed it should because the first two loops - the first two loops aren't also incrementing width, which requires 5 cycles, so of course they'll run faster! This change adds 5 cycles of nops to each loop (3 instructions - 2 rjmp+0, 1 nop). This cost 6 instruction words of flash - however, the compiler missed a chance to share the set of pop instructions between the two paths to return; doing this saved 6 instruction words, getting us back the flash the timing fix took away.
This file contains hidden or bidirectional Unicode text that may be interpreted or compiled differently than what appears below. To review, open the file in an editor that reveals hidden Unicode characters.
Learn more about bidirectional Unicode characters
Sign up for free
to join this conversation on GitHub.
Already have an account?
Sign in to comment
Add this suggestion to a batch that can be applied as a single commit.This suggestion is invalid because no changes were made to the code.Suggestions cannot be applied while the pull request is closed.Suggestions cannot be applied while viewing a subset of changes.Only one suggestion per line can be applied in a batch.Add this suggestion to a batch that can be applied as a single commit.Applying suggestions on deleted lines is not supported.You must change the existing code in this line in order to create a valid suggestion.Outdated suggestions cannot be applied.This suggestion has been applied or marked resolved.Suggestions cannot be applied from pending reviews.Suggestions cannot be applied on multi-line comments.Suggestions cannot be applied while the pull request is queued to merge.Suggestion cannot be applied right now. Please check back later.
Timeout ticked by at 16/11ths of the specified speed prior to the beginning of the pulse being measured (and, as far as I can tell, always has!)